BMWi Project ENRECO2

Increasing the energy and resource efficiency of electric steelmaking through holistic, quality guided production control

Steel pro­duc­tion is incre­asing­ly domi­na­ted by high qua­li­ty demands and requi­re­ments to redu­ce the envi­ron­men­tal impact. Espe­ci­al­ly the high ener­gy con­sump­ti­on with the con­nec­ted CO2 emis­si­ons calls for mea­su­res to achie­ve a signi­fi­cant reduction.

The pro­duc­tion of steel in an elec­tric steel­ma­king plant is per­for­med along a pro­cess chain of seve­ral steps. Steel scrap is mol­ten down in an elec­tric arc fur­nace, and the melt is refi­ned within the fol­lo­wing plants of secon­da­ry metall­ur­gy, to achie­ve the requi­red qua­li­ty for cas­ting. This one is defi­ned by tem­pe­ra­tu­re, che­mi­cal ana­ly­sis and cle­an­ness of the steel melt at deli­very to a con­ti­nuous cas­ting plant.

The over­all aim of the pro­ject was to pro­vi­de a con­tri­bu­ti­on to dimi­nish the ener­gy con­sump­ti­on of elec­tric steel­ma­king by incre­asing the ener­gy and resour­ce effi­ci­en­cy while simul­ta­neous­ly mee­ting the high qua­li­ty demands. For that pur­po­se, a through-pro­cess on-line con­trol sys­tem was deve­lo­ped. Direct savings in elec­tri­cal ener­gy were achie­ved by an opti­mal dis­tri­bu­ti­on of the ener­gy input in the dif­fe­rent pro­cess stages, using a dyna­mic ener­gy balan­ce cal­cu­la­ti­on along the pro­cess rou­te. An indi­rect reduc­tion of ener­gy con­sump­ti­on is given by savings in the alloy mate­ri­als by appli­ca­ti­on of through-pro­cess opti­mal alloy­ing stra­te­gies. Fur­ther­mo­re an impro­ved com­pli­ance with the qua­li­ty demands as well as an increased yield, lea­ding to lower ener­gy con­sump­ti­on, were achieved.

The com­ple­te sys­tem for opti­mi­sed pro­cess con­trol was imple­men­ted and tes­ted in the elec­tric steel­ma­king plant of the Deut­sche Edel­stahl­wer­ke GmbH in Sie­gen. With the help of the opti­mi­sed tem­pe­ra­tu­re con­trol the elec­tri­cal ener­gy input in the lad­le fur­nace can be redu­ced by 3.85 kWh/t. Regar­ding the con­sump­ti­on of alloy mate­ri­als savings of about 2.30 €/t can be expec­ted. The con­trol of oxy­gen input in the elec­tric arc fur­nace based on mea­su­red off-gas data led to a decrease in oxy­gen input by 10 %, con­nec­ted with a dimi­nis­hed chro­mi­um slag­ging with decreased con­sump­ti­on of redu­cing agents and slag formers.

The tar­gets of the pro­ject regar­ding ener­gy and resour­ce savings were lar­ge­ly rea­ched. It is plan­ned to trans­fer the sys­tem for opti­mi­sed pro­cess con­trol to fur­ther elec­tric steel­ma­king and also to oxy­gen steel­ma­king plants.

Report

Bran­den­bur­ger, J.; Schlaut­mann, M.; Plüm, H.-D. (BFI); Jung, H.-P.; Bei­ler, C. (DEW); Ech­ter­hof, T.; Risonar­ta, V. Y. (RWTH): Erhö­hung der Ener­gie- und Res­sour­cen­ef­fi­zi­enz bei der Elek­tro­stahl-Erzeu­gung durch ganz­heit­li­che, qua­li­täts­ge­führ­te Pro­duk­ti­ons­steue­rung, Bericht Nr. 2.31.003, BFI VDEh Betriebs­for­schungs­in­sti­tut, Düs­sel­dorf, August 2010


Logo BMWiThe pro­ject was fun­ded by the Fede­ral Minis­try of Eco­no­mics and Tech­no­lo­gy on the basis of a reso­lu­ti­on of the Ger­man Bun­des­tag within the frame­work of the 5th Ener­gy Rese­arch Pro­gram­me of the Fede­ral Govern­ment under the fun­ding num­ber 0327408A/B/C.